<Brief page summary to go here.> | ||||||||||||||||||||||||
Grumman Aircraft Engineering Corporation LOG
1. HOMBURGER VERIFIED IMU INSTALLATION NOT THE CAUSE OF ISOLATION PROBLEM. 2. TONIGHT PTA UNIT WAS INSTALLED -- ALSO NOT THE CAUSE OF ISOLATION PROBLEM. ISOLATION OK (300 Ω) TO DATE. RREA & RRAA STILL OPEN ITEMS TO BE REINSTALLED & EVALUATED. 3. RAN TDR #33 TO STEP #49. ALSO RECONNECTED P722 & PSAAM. 4. TOOK BIDDLE-DUCTER READINGS AND TORQUE MEASUREMENTS ON TDR #3 (STEPS #227 THRU #232). CONFIRMED HIGH Ω READING BETWEEN ECA 4-4 AND 4-2. REMOVED ALL MOUNTING HARDWARE AFTER TORQUE MEASUREMENT SHOWN TO BE WITHIN SPEIFIED TOLERANCES (60"/LBS +/- 5). HARDWARE & PHENOLIC COVERS HELD BY FRANK DAMIS, DEPT 053. RECOMMEND CLEAN ALL HARDWARE OF POTTING COMPOUND AND OXIDATION THEN REASSEMBLE AND RE CHECKED BY BIDDLE-DUCTER. THE COMPOSITE DATA IS AS FOLLOWS:
| ||||||||||||||||||||||||
☜ Previous page (65) | index | Next page (67) ☞ |
Advertisement
Page 66
Advertisement